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Printer killed - probbing #1345
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I'm using G29 P1 for bed levelling I'm also including my start script: M117 Heating... ;Put printing message on LCD screen M104 S140 ; set extruder temp ;G1 Z50 ; this is a good start heating position M300 S2500 P100; Beep M300 S2500 P100; Beep C108 ; Close the mesh viewer (optional) M104 S[first_layer_temperature] ; set extruder temp ; Start of print ; You may want to adjust the X and Y here so the nozzle is really above the bed! M109 S[first_layer_temperature] ; wait for extruder temp ; now print a line of filament to prepare extrusion ; Done with the dancing :) M117 Printing... ;Put message on LCD screen |
Try disabling HS mode. |
I’m having an issue with DCing. I’ve had no problems until I installed the recompile (latest) for my Ender 3v2 TCL? |
This issue has had no activity in the last 60 days. Please add a reply if you want to keep this issue active, otherwise it will be automatically closed within 10 days. |
My problem with disconnecting was solved and not related to anything. One day my Dell laptop wouldn’t boot. Blue screens of death after I added a string of lights to the USB hub. It was drawing too much current and the PC actually wouldn’t even boot. |
Did you test with a precompiled firmware?
Yes, and the problem still exists.
Bug Description
Everytime I try to do 2 prints back to back after another I always get a "Printer Killed! M112 Shutdown" and probing fail on the second print and stops the print. I have to reboot the printer and start the print again.
This is what OctoPrint is reporting:
Recv: echo:busy: processing
Recv: Probing mesh point 16/25.
Recv: T:140.00 /140.00 B:84.99 /85.00 @:18 B@:71
Recv: echo:busy: processing
Recv: Probing mesh point 17/25.
Recv: T:140.01 /140.00 B:85.00 /85.00 @:18 B@:72
Recv: echo:busy: processing
Recv: Probing mesh point 18/25.
Recv: T:140.06 /140.00 B:85.00 /85.00 @:17 B@:72
Recv: echo:busy: processing
Recv: Probing mesh point 19/25.
Recv: T:140.07 /140.00 B:85.01 /85.00 @:17 B@:72
Recv: echo:busy: processing
Recv: T:140.08 /140.00 B:85.04 /85.00 @:17 B@:68
Recv: echo:busy: processing
Recv: Probing mesh point 20/25.
Recv: T:140.05 /140.00 B:85.06 /85.00 @:17 B@:64
Recv: echo:busy: processing
Recv: Error:Probing Failed
Changing monitoring state from "Printing" to "Error"
This is my end gcode:
{if max_layer_z < printable_height}G1 Z{z_offset+min(max_layer_z+2, printable_height)} F600 ; Move print head up{endif}
G1 X5 Y{print_bed_max[1]0.8} F{travel_speed60} ; present print
{if max_layer_z < printable_height-10}G1 Z{z_offset+min(max_layer_z+70, printable_height-10)} F600 ; Move print head further up{endif}
{if max_layer_z < max_print_height0.6}G1 Z{printable_height0.6} F600 ; Move print head further up{endif}
M140 S0 ; turn off heatbed
M104 S0 ; turn off temperature
M107 ; turn off fan
This is my printer config (Ender3V2 +Sprite Extruder and a CR touch)
Send: M503
Recv: echo:; Linear Units:
Recv: echo: G21 ; (mm)
Recv: echo:; Temperature Units:
Recv: echo: M149 C ; Units in Celsius
Recv: echo:; Filament settings (Disabled):
Recv: echo: M200 S0 D1.75
Recv: echo:; Steps per unit:
Recv: echo: M92 X80.00 Y80.00 Z400.00 E424.90
Recv: echo:; Max feedrates (units/s):
Recv: echo: M203 X500.00 Y500.00 Z10.00 E45.00
Recv: echo:; Max Acceleration (units/s2):
Recv: echo: M201 X500.00 Y500.00 Z100.00 E1000.00
Recv: echo:; Acceleration (units/s2) (P R T):
Recv: echo: M204 P250.00 R800.00 T1250.00
Recv: echo:; Advanced (B<min_segment_time_us> S<min_feedrate> T<min_travel_feedrate> X<max_jerk> Y<max_jerk> Z<max_jerk> E<max_jerk>):
Recv: echo: M205 B20000.00 S0.00 T0.00 X8.00 Y8.00 Z0.40 E5.00
Recv: echo:; Unified Bed Leveling:
Recv: echo: M420 S0 Z10.00 ; Leveling OFF
Recv:
Recv: Unified Bed Leveling System v1.01 inactive
Recv: echo:Active Mesh Slot 0
Recv: echo:EEPROM can hold 5 meshes.
Recv:
Recv: echo:; Material heatup parameters:
Recv: echo: M145 S0 H195.00 B60.00 F128
Recv: echo: M145 S1 H240.00 B90.00 F128
Recv: echo: M145 S2 H245.00 B80.00 F128
Recv: echo: M145 S3 H190.00 B50.00 F128
Recv: echo:; Bed PID:
Recv: echo: M304 P133.37 I25.26 D469.46
Recv: echo:; Display Sleep:
Recv: echo: M255 S5 ; (minutes)
Recv: echo:; LCD Brightness:
Recv: echo: M256 B127
Recv: echo:; Power-loss recovery:
Recv: echo: M413 S0 ; OFF
Recv: echo:; Retract (S F Z):
Recv: echo: M207 S5.00 W13.00 F2400.00 Z0.20
Recv: echo:; Recover (S F):
Recv: echo: M208 S0.00 W0.00 F2400.00
Recv: echo:; Z-Probe Offset:
Recv: echo: M851 X-20.00 Y-40.00 Z-5.16 ; (mm)
Recv: echo:; Hotend Idle Timeout:
Recv: M86 B0 E0 S600 T170
Recv: echo:; Linear Advance:
Recv: echo: M900 K0.00
Recv: echo:; Filament load/unload:
Recv: echo: M603 L0.00 U100.00 ; (mm)
Recv: echo:; Filament runout sensor:
Recv: echo: M412 S0 D25.00 ; Sensor OFF
Recv: echo:; Model predictive control:
Recv: echo: M306 E0 P40.00 C14.40 R0.2187 A0.1257 F0.1315 H0.0056
Recv: echo:; Physical minimums:
Recv: echo: C100 X0 Y0
Recv: echo:; Physical maximums:
Recv: echo: C101 X230 Y230 Z250
Recv: echo:; Bed size:
Recv: echo: C102 X230 Y230
Recv: echo:; Mesh inset and leveling settings:
Recv: echo: C29 L25 R185 F25 B189 X5 Y5 T50 V1 ; 5x5 T=50 C
Recv: echo:; Max Extruder temperature:
Recv: echo: C104 T275
Recv: echo:; Park Head:
Recv: echo: C125 X230 Y221 Z20
Recv: echo:; Filament runout sensor:
Recv: echo: C412 M0 ; Active mode: LOW
Recv: echo:; Invert Extruder:
Recv: echo: C562 E0 ; No inverted
Recv: echo:; Probe Z Fix, Speed and Multiple Probing:
Recv: echo: C851 F0.00000 S480 M0
Recv: ok P15 B15
Full M115
Recv: FIRMWARE_NAME:Marlin 2.1.3 MRiscoC Ender3V2S1-427-BLT, based on bugfix-2.1.x (Aug 26 2024 08:49:47) SOURCE_CODE_URL:github.com/mriscoc/Ender3V2S1 PROTOCOL_VERSION:1.0 MACHINE_TYPE:Ender3V2S1 EXTRUDER_COUNT:1 UUID:cede2a2f-41a2-4748-9b12-c55c62f367ff
Recv: Cap:SERIAL_XON_XOFF:0
Recv: Cap:BINARY_FILE_TRANSFER:1
Recv: Cap:EEPROM:1
Recv: Cap:VOLUMETRIC:1
Recv: Cap:AUTOREPORT_POS:0
Recv: Cap:AUTOREPORT_TEMP:1
Recv: Cap:PROGRESS:0
Recv: Cap:PRINT_JOB:1
Recv: Cap:AUTOLEVEL:1
Recv: Cap:RUNOUT:1
Recv: Cap:Z_PROBE:1
Recv: Cap:LEVELING_DATA:1
Recv: Cap:BUILD_PERCENT:1
Recv: Cap:SOFTWARE_POWER:0
Recv: Cap:TOGGLE_LIGHTS:0
Recv: Cap:CASE_LIGHT_BRIGHTNESS:0
Recv: Cap:EMERGENCY_PARSER:1
Recv: Cap:HOST_ACTION_COMMANDS:1
Recv: Cap:PROMPT_SUPPORT:1
Recv: Cap:SDCARD:1
Recv: Cap:MULTI_VOLUME:0
Recv: Cap:REPEAT:0
Recv: Cap:SD_WRITE:1
Recv: Cap:AUTOREPORT_SD_STATUS:0
Recv: Cap:LONG_FILENAME:1
Recv: Cap:LFN_WRITE:1
Recv: Cap:CUSTOM_FIRMWARE_UPLOAD:1
Recv: Cap:EXTENDED_M20:1
Recv: Cap:THERMAL_PROTECTION:1
Recv: Cap:MOTION_MODES:0
Recv: Cap:ARCS:1
Recv: Cap:BABYSTEPPING:1
Recv: Cap:EP_BABYSTEP:0
Recv: Cap:CHAMBER_TEMPERATURE:0
Recv: Cap:COOLER_TEMPERATURE:0
Recv: Cap:MEATPACK:0
Recv: Cap:CONFIG_EXPORT:0
Recv: Cap:PROUI_AML:1
Recv: area:{full:{min:{x:0.00,y:0.00,z:0.00},max:{x:220.00,y:230.00,z:250.00}},work:{min:{x:0.00,y:0.00,z:0.00},max:{x:220.00,y:230.00,z:250.00}}}
Recv: ok P15 B15
Recv: T:33.25 /0.00 B:40.84 /0.00 @:0 B@:0
Send: M155 S2
Recv: ok P15 B15
Send: M876 P1
Recv: ok P15 B15
I'm using OrcaSlicer version 2.1.1
Anyone know what the issue could be? Once that happens the printer stops responding and can't send any other command.
Bug Timeline
No response
Expected behavior
No response
Actual behavior
No response
Steps to Reproduce
No response
Version of Professional Firmware
Marlin 2.1.3 MRiscoC Ender3V2S1-427-BLT
Printer model
Ender3V2 +Sprite Extruder and a CR touch
Electronics
4.2.7
LCD/Controller
No response
Other add-ons
No response
Bed Leveling
ABL Bilinear mesh
Your Slicer
Other (explain below)
Host Software
OctoPrint
Additional information & file uploads
No response
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